Scott, Matt, and Andrew are wiring the new bot because of our changes.
The programming team are setting up the new controller layout.
The servo was twitching uncontrollably because only the negatave wire was working.
We are innovating our bull-nose.
The middle gear is hitting the mountain while we are traveling over it.
During testing we found these problems....
- Wheels and conveyor where backwards
- The bridge servo did not have enough power to put the bridge down
- Bull-nose needs to go higher
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